The goal of this project is to create a device which can reliably and efficiently transmit heat away from a small gasoline engine and radiate it safely into the atmosphere. Heat removal is a vital component of engine design. Since many small engines serve stationary purposes with little to no air flow, it is necessary to design a device which removes heat reliably and consistently. A heat pipe will serve this purpose.
Sunday, May 29, 2016
Thursday, May 26, 2016
Week Nine Update
Week Nine Update
Pipe Sealing
This week, the heat pipe was sealed securely. Sealing the pipe has been one of the largest issues in this project. During every test prior to this, a leak developed that allowed liquid water and vapors to escape the pipe, thus reducing efficiency. This week, we tripled the amount of teflon tape on the threads of the cap and sealed the cap as tightly as possible. We then added additional teflon tape to the joint between the cap and the pipe. This proved to sufficiently seal the pipe and no leaks occurred. The increase in efficiency is apparent in figure 2 below. The pipe was set up like the other previous tests. The evaporator end was at the bottom receiving the heat. The condenser end was at the top away from the heat source. There were
three sensors. One at the evaporator end, middle and condenser end (figure 1)
Figure 1: Set up of 4th test
Test Four Results
Figure 2: Result of the 4th test
This test shows increased efficiency when compared to the last test. Once a high enough temperature is reached at the evaporator end, that end of the pipe actually begins to cool as water transfers heat to the condenser end and the radiator fins. This represents the cooling of the small engine.
Wednesday, May 25, 2016
Budget
Table:
Required Materials
Category
|
Cost
|
1” x 2’ Copper Pipe
|
$11.63
|
Aluminum Sheet
|
$12.45
|
Copper Cap
|
$2.62
|
Copper Adapter
|
$7.79
|
Brass Threaded Cap
|
$10.64
|
Distilled Water
|
$0.00
|
Epoxy Resin
|
$3.24
|
Thermal Patse
|
$4.12
|
Sponges
|
$2.16
|
TOTAL
|
$54.65
|
In the weeks following our initial materials acquisition,
the only several other expenses were made one was to get sponges to use as a
wick for the heat pipe, but those were already calculated for the final
report. The next expense is to get
thermal paste and epoxy for the heat pipe was $7.36 raising the total cost of
this project to $54.65. There should be no other expenses until the completion
of the project.
Wednesday, May 18, 2016
References
References
[1] C. E. Heuer, “The Application of Heat Pipes on the Trans-Alaska Pipeline,” U.S. Army Corps of Engineers, Hanover, NH, Special Report 79-26, 1979.
[2] W.
Wu, Y. Lin and L. Chow, "A Heat Pipe Assisted Air-Cooled Rotary Wankel
Engine for Improved Durability, Power and Efficiency", SAE Technical Paper
2014-01-2160, 2014.
[3] Single Cylinder OHV Air-Cooled Engines, Briggs
& Stratton Corp, Milwaukee, WI, 2009.
[4] G.
M. Grover, “Evaporation-condensation heat transfer device,” U.S. Patent 3 229
759, Jan. 18, 1966.
[5] SMT Component & Assembly, TutorialsWeb,
Available: http://www.tutorialsweb.com/smt/smt.htm
Timeline
Table 1: Timeline: The yellow highlights mark the progress of the group until recently.
Task
|
1
|
2
|
3
|
4
|
5
|
6
|
7
|
8
|
9
|
10
|
Research
|
x
|
x
|
x
|
x
| ||||||
CAD Designing
|
x
|
x
| ||||||||
Material Acquisition
|
x
| |||||||||
Heat Pipe Assembly
|
x
|
x
| ||||||||
Theoretical Calculations
|
x
|
x
| ||||||||
Testing
|
x
|
x
|
x
|
x
| ||||||
Data Analysis / Experimental Calculations
|
x
|
x
|
x
|
x
|
x
| |||||
Heat Sink Assembly
|
x
|
x
| ||||||||
Final Report Preparation
|
x
|
x
|
x
|
x
|
Timeline Update:
Week 7 was just completed and the pipe assembly and testing
is going on as planned for the most part, the process has been slowed because
there is also a critical defect in the heat pipe. Heat sink assembly has also been pushed to
week 8, and will be completed before the lab session. Testing will continue,
but the pipe is not working with the efficiency originally calculated. The
reason for slow progress of optimal results is due to a small leak at the
threaded end of the pipe. There is a small gap that leaks water and pressure
and in such a delicate system even the smallest gaps can negatively impact
results. So this week will be focused on solving the problem with the leak, and
assembling the heat sinks.
Week Eight Update
Radiator Fin Attachment
To attach the fins, first the surfaces of the pipe and each fin had to be prepared. Both the pipe and the fin surface were cleaned with scotch brite and methanol to remove any oil or impurities. The surface of the copper pipe was also roughened to give the epoxy more surface area to adhere to. The bases of the fins were first coated with thermal paste, then, they were held into place and secured by rubber bands. Once this was complete, epoxy was applied to the two edges of each fin. Once the epoxy for one fin had set, the next fin was begun. It was discovered that a slight bend in the middle of the bonding surface of each fin created a better fit to the rounded surface of the pipe. The rubber bands were removed after 24 hours once the epoxy had fully cured.
Figure 1: Top isometric view of the fins
Figure 2: Isometric view of the fins
Figure 3: Side view of the fins
The goal for week 8 was to get the pipe completely sealed. During the lab, the group brought the pipe over to the machine shop and got it tightened. There was, however, a little miscommunication in the group and so the pipe was only tightened but the PTFE tape was not replaced. The pipe was then tested without having the PTFE replaced and the following is the result from the test.
Test number 3
The pipe was tested again and the figure below plot out the data recorded. The difference here is that there are fins attached to the condenser end. The figures ( 4 and 5) below show the set up and the plotted result.
The result, however, does not seem to be much different than the result from week 7. The condenser also barely increased in temperature. Not surprisingly, the pipe was also leaking at the time of testing (figure 6 bellow). The team did not do a good job of securing the pipe and so the reason as to why the pipe does not work is still a mystery and the group cannot move on until the pipe has been secure tightly. The leak, however, did seem to be less than that of week 7. If the group could add more layers of PTFE and tighten the cap more then maybe the cap will be secure and result might change.
Figure 4: Set up to test the heat pipe
Figure 5: Result of test 3
The result, however, does not seem to be much different than the result from week 7. The condenser also barely increased in temperature. Not surprisingly, the pipe was also leaking at the time of testing (figure 6 bellow). The team did not do a good job of securing the pipe and so the reason as to why the pipe does not work is still a mystery and the group cannot move on until the pipe has been secure tightly. The leak, however, did seem to be less than that of week 7. If the group could add more layers of PTFE and tighten the cap more then maybe the cap will be secure and result might change.
Figure 6: Leakage of the pipe.
Week Seven Update
Radiator Fin Construction
Since the size of the radiator fins could not be reliably calculated using mathematics, it was decided to use the size and shape of the radiator fins in the CAD model. It was also decided that the material for these fins -- aluminum-- should be used for its low price and relatively high thermal conductivity.
Figure 1: Cut out of the fins
Since the sheet aluminum is very thin, it was decided that attaching the fins to their pipe would be unrealistic and would not transmit enough heat to make a difference in the performance of the pipe. Therefore, it was decided to cut the fins two at a time. Two fins would be connected together and the bent into a "V" shape with a flat bottom. Several of these "V" shapes would then be attached to the pipe with thermal paste and held into place with epoxy. This attachment will be done next week. During this week, the fins will be cut, sanded, and bent into shape.
Second Test
Figure 2: Result of the 2nd test
The heat pipe underwent a second, more thorough test to determine its feasibility as a heat pipe. The results of this test would largely dictate if the project was heading in the right direction. The results, as shown above, show a steady increase in temperature on the respective ends of the pipe as time progressed. Most importantly, the increase in temperature readings on the condenser end of the pipe shows that there is indeed a transfer of heat from the evaporator end of the pipe to the condenser end of the pipe via the wick. This is the basis of the working of the heat pipe and as per the data collected, the project will prove to be a success.
Leakage
The result was of the pipe was not as it needs to be. The temperatures at the evaporator end and condenser end are too far apart. The reason for the condenser barely going up in temperature could very much be the leakage that happened during the test.
Figure 3: Leaked water on the table after the test.
As shown from figure 3, it is a bit blended into the background but there was a leakage from the pipe during the test. This is due to the brass cap not twisted tight enough. The thread on the pipe had a few layers of PTFE and the cap was twisted on with the wrench but it was not enough.
As for conclusion, the team decided to add more PTFE layers and twist the cap on more tightly to make sure the the cap will be completely air tight. If the group could get the cap securely on, the result could be alter drastically. However, it could be that the leakage is not the main reason why the pipe does not work. This is not completely clear until this problem of the cap is fixed and tested for another time. If the water does not leak anymore but the pipe still does not work then the team has to try and diagnosed the problem.
Wednesday, May 4, 2016
Week Six Update
Modification of the pipe
From the first test last week, the pipe definitely need more testing and modification. This week, the pipe received some changes to see if a certain alteration in an element will affect the amount of heat transferred. The wick was removed from the pipe. When opening up the pipe and taking out the wick inside, there was a blue/green color to the wick.
As seen from figure 1 above. The outside of the wick has adopted a greenish color. However, figure 2 shows that the inside of the wick is normal. A member of the group made the observation and made an interesting hypothesis that the greenish color could be due to the oxidation of copper. Two facts that could back this hypothesis up is that the outside of the wick was the only thing that touched the copper pipe's inside. The fact that the copper is oxidizing is not ideal because any chemical reactions in the pipe could change the pressure of the pipe and introduce impurities into the working fluid. The pipe was then left to dry.
An alternate designed that need to be tested is the pipe without the wick. This will reveal if the designed wick was doing what it was supposed to do or not. This time, the boiled distilled water was added like last time. The threaded end of the pipe had to wrapped around with PTFE tape and then the water was poured in. The cap was then put on and tightly sealed. This get the pipe all ready for testing in lab during this week.
From the first test last week, the pipe definitely need more testing and modification. This week, the pipe received some changes to see if a certain alteration in an element will affect the amount of heat transferred. The wick was removed from the pipe. When opening up the pipe and taking out the wick inside, there was a blue/green color to the wick.
Figure 1: The outside of the wick. |
Figure 2: The inside of the wick |
An alternate designed that need to be tested is the pipe without the wick. This will reveal if the designed wick was doing what it was supposed to do or not. This time, the boiled distilled water was added like last time. The threaded end of the pipe had to wrapped around with PTFE tape and then the water was poured in. The cap was then put on and tightly sealed. This get the pipe all ready for testing in lab during this week.
Figure 3: The pipe being wrapped in PTFE tape |
Figure 4: Pouring the boiled distilled water into the pipe |
Creation of Radiator Fins
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